What a lovely review of ‘Single and Double Bed Machine Knitting; the Designer’s Guide’

November’s edition of Machine Knitting Monthly has a great review of ‘Single and Double Bed Machine Knitting; the Designer’s Guide’. Amongst other nice things, they mention the broad scope of the book’s contents. I deliberately wrote so that it is suitable for any machine owner from Brother to Passap with lots of hints and tips to work on different types of machines. Thank you Machine Knitting Monthly!

Read excerpts from the review here.

‘Single and Double Bed Machine Knitting; the Designer’s Guide’

The advance copy of my new book arrived today, and you can see some pages from the book here.

Meanwhile here is a quick look at the book.

I have made a more in depth video introduction to the book, and if you would like to watch this, please keep on scrolling down the page.

Proofreading ‘Single and Double Bed Machine Knitting; the Designer’s Guide’

I am now part way through proofreading my latest book. It’s a lot knottier checking double bed as well as single bed instructions!

The book covers, without stating the obvious, single and double bed machine knitting techniques and design. Brother,  Silver reed/Knitmaster are the main machines, but Passap machines are also included in some sections.

Step by step instructions are illustrated as well as explained in the text and at the end of each chapter there is a Design Studio exploring how to develop the techniques discussed in the first part of the chapter.

It’s got to be done before Christmas, so early mornings and late nights are the order of the day. I’m baking mince pies when taking a rest from the screen.

If you enjoyed Translating Between Hand and Machine Knitting, or are looking for the definitive book on machine knitting I think to will want this book.  You will be able to pre-order soon so keep an eye out.

‘Single and Double Bed Machine Knitting’; The Designer’s Guide‘ will be published in Spring 2023. Yippee.

Brother KH710 knitting machine refurbishment

Or

How I disassembled the needle selector plates of a KH710 and they lived to knit again

I have purchased one of these older, push-button knitting machines and at first look it was not in too bad condition. I have fond memories of these machines; Jones KH588 machines were the first ones I used at college when I started my degree in textile design in the dim and distant past. Apart from being cream rather than blue, the KH 710 is pretty similar to look at, and has the same functions and a lace carriage included. The KH710 is a little more streamlined as the two carriages have integral handles, not screw-on ones like the 588.

The 710 unpacked, de-needled and ready to be worked on

After a quick assessment it seemed to be complete and by the state of the brushes, I would say never used – but the main problems were sticking push buttons and, sadly, rusty needles. It looks like the machine may have been stored in a damp place as the needles were rusted underneath the sponge bar. This is not too bad, as the hooks and latches are not damaged so I planned to salvage as many as possible. The sponge bar itself was disgusting, melted, sticky and disintegrating into the bed, but this actually made it easier to clean it and re-line with a replacement sponge from Xena Knits. https://www.xenaknits.com/

The new sponge bar ready to go in

Before I tackled the sponge bar I removed the needles and put them into a jar of 10% citric acid for about an hour or so to see if I could shift the rust. The needles came out of the soak and after a thorough rub with wire wool and surgical spirit followed by a gentle oil they are not too bad. I’ve only had to swap a few few dire ones for fresh ones, and after a knitting test the salvaged needles knit fine. I’ve tried tuck, fair isle and slip in an acrylic 4ply and all went well.

Sample still on the machine, fair isle, tuck and slip all working OK

However, I now needed to take a look at the push buttons as some were sticking down. This started with number 8; it was very slow to rise up so the cancel button didn’t clear the selection and the needle was reselect – really annoying.

Brother apparently didn’t issue a separate service manual for the KH710, so I worked with the KH588 one I have, which was a good starting place. Although I have taken these machines apart before it was a long time ago, so I trawled the internet and found useful info on YouTube from the Answerladyknits and also from Vintage Knitting Machines. However, as with the service manual, these feature older KH585 and 588s which seem to be slightly different inside – particularly where the button module sits.

Whilst working on the machine I cleaned out the buttons, not that they were dirty, but one of the little springs was out of line, so had to be babied back into position. I may have done that whilst repeatedly testing the buttons for a clean return.

One of the parts that was difficult to get apart was the long wire that is attached to the plate which slides the button/needle selection across the bed. This is connected to the black numbered scale on the cover which shows the needle positions and has to be removed if you want to take the main back cover off. The screw is difficult to remove becasue there is nothing behind it, so no resistance to turn against. I managed to strip this and needed to use pliers in the end and a new screw was needed to replace the old one.

Since starting the refurbishment I’ve taken it apart several times and made a video which might help people with this model. I will put it on YouTube and link to it at the end of this post. The first time I removed the case, and sprayed the insides with LP1 to clean and food grade silicone to lubricate as recommended by Jack on the Answerladyknits, using both on the selector plates as well. After testing I thought the buttons were freer, but they reverted to sticking quite quickly, and had this had now moved to numbers 3 and 7. By now they were not miss-selecting but the slow return was annoying me! The physical needle selection with the set lever was also a little sluggish, so I decide the problem was probably with the needle selector plates inside the machine rather than the buttons themselves. All really frustrating. A lot of rude words were heard!

As I had taken the machine apart I thought it might be useful for other owners of 710s to see how I did this. Sadly I didn’t think of this until I was putting it back together again, but have put photos and video together to show most of my method, as you can see below.

This video explains how to disassemble and reassemble a Brother KH710 push button knitting machine. I have also made another video about unsticking sticky buttons on this machine and refurbishing rusty needles.

This video explains how to check over a Brother KH710 push button machine and the first thing to try to release sticky buttons. It also describes how to clean rusty needles and knitting to test the machine. For a more advanced fix, which includes taking the needle selector plates apart for extremely thorough cleaning, read on…
Garment pattern in tuck and stripe knit cotton yarn. Prepared in DAK 9 to be knitted on the KH710

At this point, thinking I had solved the problem I decided to knit a garment to test the machine. But whilst knitting this number 3 button began to get sticky and annoyingly slow to respond to the cancel button and pop up to neutral. It was only a little glitch, but enough to be noticeable. I also noted that number 1 and 2 were a bit slow as well. After I completed the back my frustration with the buttons overcame me and the machine came apart again.

This time I decided to concentrate on the needle selector plates. There are eight of these plates which are thin metal strips with tabs along the top, longer edge that look a bit like castle battlements. These are sandwiched between two ‘L’ shaped nesting metal needle selector plate holders in one complete assembly. Each thin plate has differently positioned, evenly spaced tabs which correspond to a push button and a needle. These plates are held in the needle selector plate holder with pins and screws and slide across each other, so must be clean and smooth without any gunge between them.

Close up of the selector plates when out of the machine, but still in their holder. In this image, plate one, which responds to button one is at the back, plate eight, which responds to button eight is at the front. This positioning depends on the way in which the needle selector holder is viewed.

The way these plates work is rather neat. Each has a different sequence of holes, (round and elongated) along their length. They also have as series of slots shaped like extended ‘U’s. When the plates are stacked together in the holder in the right order the holes overlap, forming a set of eight small holes that line up with the control wires, (or feelers) that come from the eight push buttons. When a button is pressed its feeler wire moves to the side, sliding the corresponding plate so that the tabs are inline with the needle number (1-8) to be selected. However, the plate is still too low to touch the needle butts and this is where the pins and slots come into action. When the plates are stacked in the holder, the slots fit onto the pins. As a plate slides, the slot travels over the static pin and the plate rises upwards as it reaches the higher side of the ‘U’. This lifts the tab high enough to align it with the butt of the correct needle. As the set lever is pulled the whole plate assembly slides forwards and each selected plate tab pushes the needle in front of it as it moves forward.

So I bit the bullet and stripped it down a bit more. To start with I unscrewed the white nylon zig-zag arm and removed the metal plate that slides the button selection/assembly along the bed from position 1-8. You can see how to do this in more detail in the earlier video. This allowed me to see the needle selector plates more easily. At this point the needle selector plates were still inside the machine. Next I tried taking out the three little screws on the base of the plate holder assembly which hold the right angle plate-holders together. This allowed me to open them up so that I could slide a scalpel blade between the plates to open the gaps, and squirt more LP1 into the gap and clean out any debris. I then stood the machine at 45 degrees so that the fluid would run out from between the plates and left it for an hour or so. After this the sticking improved, but didn’t go away. Plus I had a pool of lubricant in the lid of the machine that I had sat the end in… messy and smelly.

Next I decided to remove the plate holder itself. This involved removing the button assembly as well. Horrors! I was entering the dark side…

All the sensible advice is to avoid disassembling the needle selector plates, but I could see that there was a stringy, viscous substance between them preventing them sliding across each other. I really needed to clean this off! My envy of videos showing effortless button pressing on other machines spurred me on.

The selector plates being taken apart. Note the ‘U’ shaped slots and the labelling of the parts. These plates are shown with the tabs at the top, as they would be in the machine.

It all came out quite easily, which was a surprise to me. The whole needle selector assembly is mounted on three raised-head screws that enable it to slide from left to right but there is a long, screwheaded nut that fits through a metal blocking plate attached to the button assembly which stops it sliding totally off these mounting screws. I had to remove this long screwheaded blocking nut to remove the holder from the machine body. The button assembly had tocome out as well, so before going any further I carefully unscrewed the two large headed screws that hold it in place on the metal slide its rear. Once that long headed blocking nut was removed, and with a little fiddling the whole needle plate holder could be slid to the ‘keyhole’ end of the three long screw slots and holder and button assembly lifted out completely. The button wires could then be slid out of the plates and put to one side. Mine was clean, but if yours needs cleaning do that after cleaning the plates and before reassembling it all.

The long screwheaded blocking nut fitted underneath the needle selector plate holder. It fits through that metal plate so that the plate stops against a bracket, preventing the needle plate holder sliding all the way out of the raised-head mounting screws.

Now it was easy to take the plates apart. BUT, if you do this, take the time study how it all works before starting. Take lots of photos as you disassemble, and label each part clearly in permanent marker BEFORE moving it. Then if you knock things over, or have to leave the machine for a period of time, you will know how it goes back together again.

My order of work, once the holder was out of the machine, was a follows:

Remove the inner plate holder

Label L and R end

Remove all the plates in one go and lay them parallel to the inner with the tabs facing away from you

Label the outer holder L and R.

Carefully separated the top needle selector plate

Label it on one end. I used ‘L1’ meaning it is push button 1, and that that end matches ‘L’ on the holders. All others followed as ‘L2’, ‘L3’ etc. One is the plate at the rear of the holder, eight is the one at the front.

Wipe the plate clean of oil and dirt and polished both sides

Replace it onto the pins in the outer holder, matching L to L.

Repeat with each plate, making sure to label them methodically.

Test that the plates slide smoothly.

Screw the holder back together.

Phew, time for a cuppa now!

With a little fiddling the button wires went back into their respective holes. I found this easier to do with the assembly held so that the wires were vertical.

Sliding the button wires back through the selector plate holes

Because that long screwheaded blocking plate nut is really awkward to replace in situ I replaced it in the needle plate holder before putting it back into the machine. This meant that I had to remove one of the raised screws which the holder slides on otherwise the blocking plate didn’t fit correctly and the holder would not slide. These raised screws attach through to the set lever mechanism, but temporarily removing the left hand one, (button side of the bed) meant that I could slide the needle selector holder and button assembly back in place so that the blocking plate and nut fitted together correctly and did their job. Just remember to replace and fasten this screw before you move anything else.

A quick test showed that the buttons were zapping away cleanly and efficiently and that the needles were selecting with ease. After that is was plain sailing, and the machine went back together as shown in the original videos without any problem.

I hope this might help anyone who wants to take a Brother KH710 apart for repair. I certainly could have done with a bit of help.

I will put this into a pdf at some point and upload it here.

Machine Knitting workshop, Brighton TAG

Today I ran a workshop that introduced members of Brighton Textile Art Group to machine knitting. To give a wider experience both a Knitmaster and a Brother machine were used, one standard and one chunky gauge. The chunky was particularly popular once it was found that it can knit handspun yarns.

Techniques explored included shaping, fair isle, single motif fair isle, knitwear (again great for hand spun), holding and short rows and simple, manual lace transfer.

I took along a little circular machine to demonstrate the difference between the two machine types, but the real interest was in the flat bed Japanese machines.

After the workshop response were really positive; people who had thought they would hate it had great fun, and those with machines were enthused to go home and get them out. Unfortunately the workshop clashed with the East Sussex Guild of Spinners, Weavers and Dyers meeting, so another workshop had been requested in the Spring or Summer of 2020.

Talk in March 2020

I will be talking to Long Buckby Machine Group next March about my career in knitted textile and knitwear design, and the inspiration behind ‘Translating Between Hand and Machine Knitting’.

I’m looking forward to meeting members of this well-established machine knitting group.

Brother KH260 chunky knitter being a cranky machine

There is only one photo to go with this post as I was so covered in oil I didn’t feel secure holding a camera!

I am running a machine knitting workshop for my local Brighton and Hove Textile Art Group (TAG) in a few weeks, and most uncharacteristically I decided to plan in advance and check out the machines I will be taking along.

TAG is affiliated to the East Sussex Guild of Weavers, Spinners and Dyers, so most members spin in one way or another (drop spindle or wheel), so knitting hand spun yarn seems a pretty sensible thing to cover in the workshop. Because of this I intend to take my Brother KH260 chunky, single bed machine. I do love this machine, but haven’t used it in several years. Whilst I was working on ‘Translating Between Hand and Machine Knitting’ I used my two electronics, a Knitmaster mid-gauge HK160 and a Knitmaster punchcard, so there just wasn’t room for the 260 to be out. Since completing the book I have been diverted to spinning and dyeing for a refreshing change, hence the long storage of the KH260.

When I unpacked the machine it was frustrating to find that the timing belt seemed jammed. The carriage would knit fine in stocking stitch mode, but everything else refused to work. Luckily my long experience at machine maintenance stood me in good stead to sort out the sticking cams on the carriage which were preventing the KC dial from activating and connecting the carriage to the timing belt, taking the machine cover off to expose the workings at the back, and understanding the basics of the patterning mechanism. For a start, the carriage and pattern mechanism parts were all covered in yellow, thick gloopy oil that I know glues the workings of the machines when they are left unused, so I applied LPS1. After watching many of ‘TheAnswer Lady and Jack’ YouTube videos when working on various machines I had invested in a can of this spray cleaner/lubricant; it works really well and is to my mind well worth the rather high cost (in Europe, not sure about elsewhere). According the Jack, LPS1 does not damage the plastic parts of the machine like mineral oils do and is similar in chemical composition to the Bellador oil supplied with Passap machines.

Having replaced a broken Brother timing belt before I’ve found its quite a long and exacting job so I am wary of timing belts and did not want to stretch or break this one whilst sorting out the problem. The service manual (downloadable from the wonderful resource at machineknittingetc.com) is really useful, but I still couldn’t work out what was jamming the belt. So it was back to ‘The Answer Lady’ and Jack, who is a fount of all knowledge on knitting machines.

After watching two of their helpful videos about the Brother timing belt I was pretty sure that the problem was connected to the right hand end of the belt and the associated cog and cam. On the right of the card reader, there is a round cog with a spring on the top that the timing belt goes around and inside this there are cams that activate the patterning mechanism; this clog refused to move more than a third of the full revolution, and felt ‘sticky’. So I soaked it in LPS1, making sure to get the little tube over the holes so that the spray would penetrate fully into the enclosed middle. But 24 hours later it was still stuck, but the black roller rotated, and now the card roller knob popped up and down when the cog mechanism revolved the short distance it was able to, but this still jammed after a third of a revolution.

After a further trawl of YouTube I found another, slightly older video that discussed reasons why the pattern mechanism won’t advance in a bit more detail. In this video, Jack explains that a drive cam hidden underneath that right hand, cog mechanism rotates the lower of the two card mechanism rollers (the white plastic one), which I had already noticed was not revolving when the top (black) one did. I now knew that the problem was definitely under that right hand mechanism. More LPS1 went into it; the machine case was now awash with the stuff! After another hour or so soaking the time had arrived for another test run.

With a rag to help my grip I nudged the clogged mechanism into a place it didn’t want to go. I could feel the gunk fighting me, but it was slowly yielding, and most importantly, as I nudged it, the lower, white roller began to revolve. I was now certain that the hidden cam was stuck up with gunk, and needed to be helped to free itself. I connected the carriage to the timing belt by setting it to KC, and if I gently moved this in the right direction I could add a little more leverage – gentle was the word here, remember my fear of damaging the timing belt? More LPS1 went in, and a bit more nudging back and forth, and slowly it all began to free-up. At last the cam gave and the clogged mechanism moved fully, the lower roller rotated and the punchcard mechanism advanced!

Wooppee!

Next came a test with a punchcard, which seemed to select needles and rotate OK. It took several rags to mop the LPS1 out of the case; it was leaking a bit and I didn’t want it to run out on the floor when I put the machine back on its end for storage.

Before putting the case back on I tested the patterning by knitting a piece, which worked up no problem. I felt wonderful – its such a kick mending something.

Those oily rags then came in useful to wipe off all the yellow gloopy oil that was left on parts of the inner workings of the machine. After that the case went back on. I’d reserved an oily rag to wipe down the beds and other exposed metal parts to protect and lubricate the machine; we live near the sea so I am very conscious of the rust factor. My old Knitmaster 700 had a rather sad case of rust when I was bequeathed it, but LPS1 was a great help in restoring it to good health.

I now have a working KH260, shiney and ready for the workshop. On to the next machine…

The Answer Lady and Jack videos can be found on YouTube, and these were the ones I used to help me with this problem.

Several Reasons why a Brother card reader might not advance, The Answer Lady and Jack, on YouTube.